Page 11 - PEN Ebook May 2021
P. 11

Cover Story - Design                                                                    Cover Story - Design


                                                                                Figures 5 and 6 show the effi-

                                                                                ciency of the presented demo
                                                                                board. The measured efficiency
                                                                                includes the bias consumption
                                                                                but not the power consumption
                                                                                of the fan. Regarding the input
                                                                                current performance, the pow-
                                                                                er factor is over 0.95 when the
                                                                                load is higher than 20 percent of
                                                                                the nominal output power and

                                                                                a THD under 5 percent for an
                                                                                output power over 50 percent of
          Figure 4: Prototype of the 3.3 kW totem-pole PFC board implemented with
          CoolMOS™ CFD7 and S7 SJ MOSFETs.                                      the nominal one. The maximum
                                                                                efficiency is over 98.9 percent in
          after t . For this case, the pulse applied to the    the range of 1000 W to 1500 W output power and
                6
          pre-charge MOSFET Q3 becomes effective and           over 98 percent for the measured power range.
          causes the charge of Q1 C OSS  to the depletion      With the CoolMOS™ CCM totem-pole PFC solution,

          voltage by the C HS_DP  –Q3-D1-Q1 network. Once      the next level of silicon-based efficiency can be
          Q2 is turned on, its drain-to-source voltage will    reached, making it a cost-attractive alternative that
 Figure 3: Commutation waveforms of the proposed solution.  drop again close to zero, and a smooth transition   complements our powerful offering of wide-band-

 As depicted in Figure 3, the pre-charge current   When the PWM B signal goes low, similarly as   “switch to diode” is achieved without severe hard   gap solutions.
 waveform has two peak pulses, the first one,   before, due to the Ry-Cy network at the input   switching.
 between t  and t , is related to the charging of the   of the gate driver of Q1, there is a certain delay
 3
 2
 Q2 C OSS , and the second one (with a lower mag-  before the device entirely turns off at t . Due to
 5
 nitude) between t  and t  is due to the resonance   the load or inductor current, immediately after   EXPERIMENTAL
 4
 3
 with the stray inductances of the pre-charge loop.  the channel is completely closed, the C OSS  of Q1   RESULTS ON
 will be charged to 400 V, and the C OSS  of Q2 will   INFINEON’S DEMO
 When the delayed PWM B signal finally reach-  be discharged to 0 V producing a ZVS transition   BOARD
 es the gate of Q1 at t , the C OSS  of Q2 is already   for Q2. This is the case of the “switch to diode”   The concept presented in this
 4
 depleted with 20~24 V, which sets the stage for a   transition in a PFC application. In this situation,   article has been tested in a
 diode-to-switch smooth transition.  the pre-charge circuit of the high-side switch   3.3 kW totem-pole bridgeless
                                             Table 1: Infineon products used in the 3.3 kW totem-pole evaluation board with Si
 (C HS_DP -Q3-D1) will not influence the operation of   PFC, switching at 65 kHz and   SJ CoolMOS™
 The pulse duration applied to the pre-charge   the half-bridge with Si SJ MOSFETs.  using SMD components.

 MOSFET Q4 goes beyond t  when commutation                     CONCLUSION
 4
 and transient events happen in both Q1 and Q2.   This ZVS turn-on transition of the diode is pos-  The demo board shown in Figure 4 is a system   Using a simple and effective pre-charge circuit,
 This is done intentionally to guarantee the proper   sible when the load or inductor current is high   solution from Infineon Technologies and imple-  which allows the depletion of the Si SJ MOSFETs
 losses of the Si SJ MOSFET Q1 during turn-on. If   enough to allow the charge and discharge of   ments the power switches, diodes, drivers, and   and thus brings Q OSS  and Q  losses to a minimum,
                                                                                         rr
 this pulse falls short, the possibility to have se-  the corresponding C OSS . However, if the inductor   controller presented in Table 1. The pre-charge   Infineon now enables the usage of Si SJ MOS-
 vere hard commutation is high in the Si SJ MOS-  current at this transition is not enough to charge   circuit has been designed according to [5], and   FETs in CCM totem-pole PFC applications.
 FET, which would produce destructive results if   and discharge the C OSS  of the half-bridge devic-  it is implemented according to the design values
 it occurs during long periods. Similarly, the LV   es, a hard-switching transition will happen. This   compiled in Table 2.  This article demonstrated the working principles
 MOSFET could run continuously in avalanche.  situation is shown in Figure 3 as a dotted line   of this innovative concept and the experimental


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