Page 9 - PEN Ebook May 2021
P. 9

Cover Story - Design                                                                    Cover Story - Design


          ductor connected to the switching node. However,     At a given moment in time (t ), Q2 must be
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          when Q2 is turned off, the inductor current keeps    switched off so the current will flow again
          flowing through its body diode, and, when Q1 is      through Q1 when turned on. After a certain delay
          turned on, a hard-commutation of the body diode      time (due to the R -C  network at the input of
                                                                                y
                                                                                   y
          current occurs, leading to catastrophic results. By   the gate driver of Q2), the gate-to-source volt-
          applying the proposed solution, the Q  is removed,   age signal of Q2 also changes its state to off at
                                              rr
          and at the same time, the charge in the output       t . During the mandatory dead time in any half-
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          capacitance (C OSS ) of Q2 Si SJ MOSFETs is consid-  bridge (t -t ), the inductor current freewheels
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          erably reduced, and so its associated losses.        through the body diode of Q2. During this time,
                                                               the switching node is clamped to the ground,

          The included R -C  and R -C  filter networks at      with voltage drop –V BD-Forward . Also, all the boot-
                           x
                        x
                                     y
                                  y
          the driver inputs allow the proper timing of the     strap capacitors, except for C HS_DP , for both driving
          PWM signals to the half-bridge devices and the       and depletion voltages are charged.
          added LV switches; thus, no extra PWM signals
          from the controller are required.                    Then, after the corresponding dead time, PWM B
                                                               is applied, and the CXRX network at the input of
          The circuit diagram in Figure 2 depicts a typical    the Q4 gate driver generates a pulse of a particu-

          double-pulse test platform using the proposed        lar duration. At t , the pre-charging MOSFET Q4 is
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 Figure 2: Circuit diagram of the proposed solution using CoolMOS™ in a half-bridge configuration.  solution. This setup configuration reflects the   turned on, and a pre-charge current (pre-charge I
          same situation of “diode-to-switch transition”       “diode”) circulates in the C LS_DP -Q4-D2-Q2 net-
 To overcome these difficulties and make it pos-  transition since those charges are provided from   in the totem-pole PFC operating in CCM where   work. The effective circulation of this current
 sible to use Si SJ MOSFETs in half-bridge CCM   a low voltage source. The result is a significant   hard-commutation of the “diode mode” switch   depends on the fact that the magnitude of such
 operation, Infineon Technologies has developed   reduction in the commutation losses in the Si SJ   occurs every switching cycle.  pre-charging current must be higher than the
 and implemented an attractive and straightfor-  MOSFETs. Also, continuous hard-commutation in   freewheeling load current flowing through the
 ward solution. The innovative prototype achieves   the normal CCM operation of the totem-pole PFC   body diode of the Si SJ MOSFET Q2. At the end
 the highest efficiency in CCM totem-pole PFC   is now feasible.  HARD COMMUTATION   of the pre-charge current (t ), the intrinsic body
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 topology at an attractive price-performance ratio.   TRANSITION WITH THE   diode of Q2 is deactivated, and the drain-to-
 In the following sections, we present the working   The proposed “pre-charge” solution requires a   PROPOSED SOLUTION  source voltage (V DS,Q2 ) is pre-charged to 24 V, thus
 principles and the measured experimental results   single high-voltage Schottky diode (D1 and D2 in   Figure 3 presents the main waveforms happening   bringing the following benefits:
 of our system solution.  Figure 2), a low voltage (LV) MOSFET (Q3 and Q4   during the commutation of a half-bridge imple-
 in Figure 2), and a capacitor (C HS_DP  and C LS_DP ) per   menting Si SJ MOSFETs Q1 and Q2. For readers’   ▶   This pre-charge voltage brings the half-
 power device in the half-bridge, as well as two   convenience, the time axis showing the transi-  bridge capacitance closer to the knee of the
 HIGH-FREQUENCY HALF-BRIDGE   supply voltages, for driving the LV MOSFET and   tions that occur at the different PWM events is   non-linear C OSS  curve (Figure 1).
 OPERATION PRINCIPLE WITH SI   providing the pre-charge voltage. The solution also   not in scale.
 SJ MOSFETS  implements a level-shifting (bootstrap capacitors)   ▶   The commutation losses at this point are

 With the proposed solution, the C OSS  capacitance   technique, with traditional drivers for both the   In a previous state than t , the inductor was en-  considerably lower than in the point where
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 of the freewheeling or “diode mode” (Q2 in Figure   driver supply and the depletion voltage (highlight-  ergized through Q1, which would implement the   the drain-to-source voltage is negative or
 2) Si SJ MOSFET is pre-charged at a certain level,   ed in orange and grey, respectively, in Figure 2).  switch function in a totem-pole PFC. Once Q1 is   close to zero. Without the pre-charging,
 e.g., 24 V (Figure 1). This pre-charging drastically   turned off, the inductor current flows through   the losses would include the body diode Q
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 reduces the losses associated with its output ca-  In the half-bridge configuration of Figure 2, Q2   Q2, first through its body diode and then through   losses and the very large output capacitance
 pacitance charge (Q OSS ) and the reverse recovery   typically turns on with soft-switching after Q1   the channel of the device, once Q2 is turned on.  associated Q OSS  losses of Q2.
 charge (Q ) of its body diode during the turn-off   turns off, given the energy accumulated in the in-
 rr
 8  MAY 2021 | www.powerelectronicsnews.com                            MAY 2021 | www.powerelectronicsnews.com       9
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